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Casting Failure Investigation

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BACKGROUND
Two (2) partially machined impellers cast from C95200 aluminum bronze were submitted to our laboratory for casting failure analysis. The submitted castings identified as #1 and #3 exhibited casting surface defects primarily associated with the middle to OD sections of the impeller vanes.

Casting of the impellers was reportedly performed in a steel mold that utilizes six furan cold box cores. The six core segments were assembled using core mud, banded, fitted with a ring and dried. Final processing of the core package included a graphite dip followed by drying in an oven. Hot metal at 2200ºF was introduced into the molds using low-pressure vacuum from the furnace. Metal from the sprue feeds into the drive hub, which is in the drag of the casting. Venting was reportedly from the OD of the mold. The casting, mold, and venting design are new. We were requested to determine the casting defect root cause.
 
SAMPLE IDENTIFICATION
Description Material Sample ID
Cast Impellers CDA C95200 Aluminum Bronze Casting (#1) and Casting (#3)
 
PERFORMED TESTING
Visual and Stereoscopic Examination
Metallographic (Microstructure) Examination
Energy Dispersive Spectroscopy (EDS)
Chemical Testing
 
CONCLUSIONS
1. Based upon the performed metallurgical failure investigation, it is our opinion the casting defect root cause was insufficient venting of gas within the molds produced from the reaction of the hot metal and cold box cores.

2. The exterior and interior profiles of the defects consisted of folded metal with foreign material that was entrapped along the boundaries of the folds during solidification. The foreign material was identified as containing a major elemental concentration of sulfur.

3. The source of the sulfur was most likely the SO2 used as a catalyst in the making of the six cold box cores. Pressure build-up of gas released from the cores during fill of the mold resulted in excessive metal turbulence that formed numerous metal folds during solidification. The narrow solidification range of the aluminum bronze provided less time for proper venting of the reaction gas containing significant amounts of sulfur.

4. Visual and metallographic examination of the defect profiles revealed irregular surface wrinkles and subsurface folds of metal. Casting #1 exhibited the most severe defects, which on vane #2 extended through the full thickness of the vane. Metal folds and surface irregularities on casting #3 were predominantly confined to the surface, which were measured to a maximum depth of .010 – .012”.

5. The microstructure of the two castings consisted of an “as-cast” alpha and beta structure, which was characteristic of C95200 aluminum bronze. The foreign film lining the boundary of the defects appeared as gray to dark gray in appearance. No evidence was observed of any shrinkage cavities.

6. Energy dispersive spectroscopy (EDS) analysis of the foreign material lining the defects revealed a major elemental concentration of sulfur, which is not an element common to C95200 aluminum bronze.

7. The sulfur content of casting #1 was determined by chemical testing (OES) at < .005%, which indicated the sulfur detected in the material lining the metal folds was from a foreign source; most likely the furan cold box cores.

8. We respectively recommend that the venting design of the mold be reviewed to provide maximum release of gas produced from the cold box cores. Additionally, verify that proper procedures are followed during blow of SO2 as catalyst during the production of the furan cold box cores to minimize reaction products formed in the mold during fill.
 
SUMMARY of TEST RESULTS
Visual & Stereoscopic Examination
1. Visual and stereoscopic examination of Castings #1 and #3 revealed surface wrinkles and irregularities primarily associated with the middle to OD sections of the impeller vanes. The appearance of the wrinkles and irregularities suggested abnormal turbulence of metal within the mold cavity contributed to formation. (See Photos 1 – 4 on the following page)

2. Surface defects on vanes 2, 3, and 4 on Casting #1 and vanes 5 and 6 on Casting #3 were sectioned for metallographic examination of the defect profiles.
 
Casting Failure Investigation
Photo 1: View of Casting #1.
 
Casting Failure Investigation
Photo 2: View of Casting #3.
 
Casting Failure Investigation
Photo 3: View of defects on vane #2 of Casting #1.
 
Casting Failure Investigation
Photo 4: View of defects on vane #6 of Casting #3.
 
Metallographic Examination
1. Metallographic examination of the defect profiles revealed irregular surface wrinkles and subsurface folds of metal. Casting #1 exhibited the most severe defects, which on vane #2 extended through the full thickness of the vane. (See Photos 5 and 6)

2. Metal folds and surface irregularities on casting #3 were predominantly confined to the surface, which were measured to a maximum depth of .010 – .012”.
 
Casting Failure Investigation
Photo 5: Mag: 50X; Etchant: None View of defect profile of Casting #1 at the surface of vane 2.
 
Casting Failure Investigation
Photo 6:Mag: 50X; Etchant: None View of defect profile of Casting #1 at the mid-wall of vane 2.
 
Casting Failure Investigation
Photo 7: Mag: 100X; Etchant: NaOH4 + H2O2 View of defect profile of Casting #3 at the surface of vane 6.
 
Casting Failure Investigation
Photo 8: Mag: 500X; Etchant: None Close-up view of foreign material that lined the defect profiles. The material was subjected to EDS analysis.
 
Energy Dispersive Spectroscopy Analysis
1. EDS analysis of the material lining the boundaries of the interior defect profiles of both samples revealed major elemental peaks of sulfur (S), aluminum (Al), copper (Cu) and a minor elemental peak of iron (Fe). Aluminum, copper, and iron are common to C95200 aluminum bronze. However, sulfur at high levels is not common to aluminum bronze.

2. The most likely source of the high level of sulfur is the furan cold box cores.

3. The EDS spectrum is shown in attached Figure 1.
 
Chemical Testing
1. Chemical test results of Casting #1 verified the sample as C95200 aluminum bronze.

2. The sulfur content of the casting was determined at < .005%, which indicated the sulfur associated with material lining the metal folds (defects) was from a foreign source.

3. The results are shown in attached Table 1.
 
Respectfully Submitted,
MSi Testing & Engineering, Inc.

Allan W. Scheive
Senior Metallurgical Engineer
Reviewed By,


John J. Fruscione
Senior Metallurgical Engineer
 
Figure 1: EDS spectrum of the material lining the defects of Casting #1.
 
Table 1 – Chemical Testing*
Copper = 86.6  %
Aluminum 8.9
Iron 4.0
Sulfur <.005
Grade C95200
* Testing performed in accordance with MSi Procedure No. 1002.
 

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